邓铭江,胡智农,贺建国,穆汉平,卢安琪. "635"水利枢纽发电引水洞混凝土腐蚀机理分析[J]. 水利水运工程学报, 2000, (3): 38-42.
引用本文: 邓铭江,胡智农,贺建国,穆汉平,卢安琪. "635"水利枢纽发电引水洞混凝土腐蚀机理分析[J]. 水利水运工程学报, 2000, (3): 38-42.
DENG Ming-jiang,HU Zhi-nong,HE Jian-guo,Mu Han-ping,LU An-qi. Analysis on corrosion mechanism of shaft weel concrete for "635" hydro-power project[J]. Hydro-Science and Engineering, 2000, (3): 38-42.
Citation: DENG Ming-jiang,HU Zhi-nong,HE Jian-guo,Mu Han-ping,LU An-qi. Analysis on corrosion mechanism of shaft weel concrete for "635" hydro-power project[J]. Hydro-Science and Engineering, 2000, (3): 38-42.

"635"水利枢纽发电引水洞混凝土腐蚀机理分析

Analysis on corrosion mechanism of shaft weel concrete for "635" hydro-power project

  • 摘要: “635”水利枢纽发电引水洞竖井段围岩中 ,有黄铁矿脉风化形成的黄钾铁矾化蚀变带通过 .经对竖井衬砌混凝土腐蚀破坏机理的分析后认为 ,必须采用有效的防腐材料 ,将混凝土与侵蚀介质隔离开来 ,对竖井混凝土进行防腐蚀处理 .

     

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